Sistema di sospensione MORryde CRE2-35 CRE3000, assale in tandem - interasse da 35 pollici

Brand:MORryde

3.8/5

382.74

Quando si tratta di prestazioni delle sospensioni, tutto dipende dalla corsa delle sospensioni. Una maggiore corsa significa un traino più fluido, una migliore trainabilità e una migliore protezione dai dannosi urti della strada. Il MORryde CRE3000 offre oltre 3 pollici di escursione della sospensione. Al centro di questo sistema di sospensione c'è un inserto in gomma compressa insieme a uno slot di viaggio unico per aiutare la tua unità a scivolare dolcemente sulle strade accidentate di oggi. Il CRE3000 offre anche una maggiore durata e una riduzione dello stress del telaio. È stato testato e valutato per l'uso con assi fino a 8K; è costruito per durare! L'installazione è semplice e diretta e può essere eseguita da un rivenditore, un centro di assistenza o qualsiasi fai-da-te.

Testato e valutato per assi fino a 8K. Facile installazione imbullonata. Protegge dai dannosi urti stradali. Fornisce 3 pollici di corsa della sospensione. Traino più fluido rispetto alle tradizionali molle a balestra.
Brand ‎MORryde
Customer Reviews 4.8 4.8 out of 5 stars 677 ratings 4.8 out of 5 stars
Item model number ‎CRE2-35
Item Weight ‎8.23 pounds
Manufacturer ‎Morryde
Manufacturer Part Number ‎CRE2-35
Model ‎CRE2-35
OEM Part Number ‎CRE2-35

3.8

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Scritto da: Mathew K Raikes
Glad I did it
In short, I bought this. Installed it myself. Survived the experience. Glad I did it. Want a ridiculous amount of detail? Keep reading. PLEASE NOTE: Below I refer to parts that are part of MORryde’s shackle kit and NOT with the CRE3000 alone. Don’t think you’ll be able to do everything I describe below with only the CRE3000. On impulse I decided to upgrade the suspension on my 2006 26' travel trailer. Myself. In my driveway. I've never done anything like this before, but how hard could it be? So without revealing to my wife my grand plan to turn our driveway into an RV maintenance yard, I ordered the CRE3000 and (since I'd be removing the wheels and rusty bolts anyway), I decided to upgrade the shackles as well with the MORryde heavy duty shackle kit. I think it's called "wet" because you can lubricate it. (MORryde UO12-016 Heavy Duty Shackle Upgrade Kit, CRE3000 / Stock / Equaflex 2.25" Shackles - Tandem Axle . Additional stuff purchased, using this project as an excuse, included: A 2 ton floor jack with a 23+ inch lift (enough range to lift my trailer at the frame). A grease gun (for the zerk fittings on all the new boltsGreaseTek Premium Pistol Grip Grease Gun with 18" Hose and Extension Pipe ). A 24" breaker bar (rusty bolts are fun!). A can of B'laster (B'laster 16-PB Penetrating Catalyst - 11-Ounces . A set of impact sockets for my air powered impact gun. Two tall jack stands (tall enough to support the frame jacked up). Some work gloves. Additional stuff I used that I already had on hand: An air compressor. Air powered impact gun (pretty excited about my 2nd opportunity to use it in 10 years). A second, much smaller floor jack (I didn't expect to use this, but it was VERY handy to have - details below). A creeper/crawler borrowed from a neighbor. Two small jackstands for supporting the disconnected axles. A couple wrenches of appropriate size for my bolts. A rubber mallet. A hammer. A punch. I planned to tackle the project with my 13 year old able assistant on a Saturday afternoon. So starting Thursday, I began soaking the eleven year old bolts/nuts (7 on each side of the trailer) with B'laster hoping to make them easier to remove after a couple days of soaking. Saturday afternoon I hauled the trailer out to the driveway, jacked it up, placed the two tall jackstands to support the trailer, and removed the two wheels (on one side), revealing the entire suspension. Then, thinking it might take a some pressure off the leaf spring and bolts, I lifted each axle just a little bit and supported them with small jackstands. Now it's time to remove those rusty old bolts. So the bolts faced away from me. That is, they were inserted with the head toward the outside and the nuts on the inside (under the trailer). No problem. I put a wrench on the backside to hold the nut in place, and then used my air-wrench to turn the head. Or tried to. Didn't budge the tiniest bit. Then I hung my 13 yr old off the end of the breaker bar. Then I hung myself off the end of the breaker bar. Didn't budge the tiniest bit. More P'blaster, a little banging with a hammer to try and free the frozen bolts. No joy with any of the 7 bolts. I was extremely frustrated and had to really bite my tongue to avoid language my assistant shouldn't hear. Until one bolt finally gave just a little bit. At this point, some of you more knowledgeable folks already know my mistake. It turns out the bolts themselves (on my trailer) aren't intended to turn. Near the head of the bolt is a small area of grooves that locks the bolt in place. The nut has to be removed from the stationary bolt. At least until the nut backs off far enough that the bolt can be tapped out past the grooves and then turns as you might expect. So learn from my mistake - apply pressure to the nuts, not the bolts. I wish I had learned this lesson an easier way, say by looking at the brand new replacement bolts, seeing the grooves and realizing their obvious purpose. But that's not my style. Plus it was a lesson in perseverance for my assistant. If at first you don't succeed, cuss, hit it with a hammer, nearly give up, and then get lucky. Anyway, after the bolt design revelation things started moving much faster. Between the air-gun and breaker bar all the nuts came free without too much difficulty. The creeper and small size of my assistant (compared to me) was invaluable in removing the nuts under the trailer. Thank goodness for sturdy jackstands and his mom staying in the house. Then we used a punch to knock the bolts out, freeing the leaf springs and removing the triangular center hanger. More use of the punch to push the worn OEM plastic bushings out of all the bolt holes. Now disassembly is complete. Reassembly was mostly straightforward. Insert the shiny brass bushings (from the shackle kit) into all the bolt holes and gently tap in with rubber mallet. Hang the new CRE3000 in the center and drive in the center bolt, put the nut on the back, but not tight yet. Reattach the leaf springs to the left & right of the CRE3000 using the new shackles and bolts from the kit. One tip - on the center bolt (that hangs the CRE) the zerk fitting in the head of the new bolt faces outward toward you. On ALL other bolts, the zerk fittings face inward, under the trailer. That's supposed to make it easier to reach and lube when the tires are on. So unlike the original bolts, all the nuts except the center bolt will now be on the outside rather than inside. That'll be handy in the future when I forget the lesson learned above. The left & right ends of the leaf springs that attach to the front & rear frame hangers can be a little tricky to get aligned so the bolts will go through. The holes will be too high, too low, or crooked. This is where I used my small floor jack to push up on the end of a spring raise it, or push down on the spring to lower it. To push down on the spring, I set the jack on TOP of the spring and pumped it up until the jack foot hit the frame above. Than as I continued to pump, the jack pushed the spring down aligning the holes. It took a bit of fiddling, including with the axle jack stand, to get the leaf spring ends reconnected, but in the end it wasn't really hard. The last step was to tighten all the nuts and lubricate the 7 bolts with the new grease gun. Then we we replaced the tires and we were done. With one side. It had taken us about 4 1/2 -5 hours and daylight was running out. We finished the job the next day and, with the lessons learned, it took only about 2 1/2 hours to finish the second side. So roughly seven hours total including the time penalty for stupidity. We went for a test drive and I immediately noticed two things. First, the tires/axles didn't immediately fall off. That was a relief. My mind had been full of "what ifs" and "what did I forget?" and "where did that extra bolt come from?" (just kidding). The second thing was how QUIET the trailer was. I had gotten used to lots of squeaks and squeals over speed bumps and maneuvering at low speed, but now the trailer is whisper quiet in all circumstances and seems to float along behind the truck rather than bounce. I'm very pleased with the end result and glad I chose to do it as a DIY. It was actually a very satisfying project to complete with my son.
Scritto da: Carla Richards
Packing needs improvement
New slices cardboard they are using for packing doesn’t prevent these heavy parts from moving around. Results in chipped paint and scratches that could be taken as used. Other than that appears to be nicely made.
Scritto da: Cust8e0
Get them !
I looked everywhere to get instructions for where to jack up my travel trailer. No-one wants to tell you where the jack points are. My tow behind trailer weighs 7000 lbs. I put 6 ton bottle jack behind back wheel and lifted up till both tires (on same side) were clear of ground, by about an inch. Then I put a 6 ton jack stand as close to bottle jack as possible and lowered jack onto that stand. Then I repeated same thing on other side of trailer. Now all 4 wheels are hanging. Getting the brass bushings into each spot is easy, getting the CRE installed to its 3 bolts is easy. Getting the spring re-installed to the trailer frame took all day. What I ended up doing was loosening the 4 bolts that hold the axle to spring pack and gave me just enough play so I could rotate the spring 1/8"?? inch and thats all it took to get the spring bolts back in. I then retightened the spring-pack bolts. I made a mark on the axle before removing those bolts so I would be sure to line up axle with spring pack at re-assembly. Never needed that mark, there was no movement. First test was speed bump in my neighborhood. My F350, both front and back axles, made me well aware there was a bump. Trailer gave ZERO hints it hit a speed bump. I looked in mirror to see when my trailer wheels would hit it and I was already past it. Amazing ! When docking at our campsite, it would creak and groan during maneuvering. That is now gone. If I did this again, I would loosen the pack bolts early and I expect I could finish one side in 1/2 hour, MAX. As I was right there, I elected to re-pack the wheel bearings and that takes time and a zillion rags. Oh, about the 6 ton bottle jack. Do you need it ? No, I have a 3.5 ton floor jack and it worked but it was VERY difficult to pump. I also have a 4 ton bottle jack and it was tough to pump up. The 6 ton bottle jack was a breeze to pump. Consider getting "buddies" for your bottle jack. Look up "safe jack DOT com" accessories.
Scritto da: Blackwell 315
Major difference!
This product is a must to replace the stiff, original suspension. Installation did take a while, and plenty of patience was required matching up the holes between the frame and leaf springs, but it is worth it! Installation took roughly 6+ hours, which also included re-greasing the bearings. If you have a level concrete base, it will be a breeze when moving around the floor jacks, installing on dense grade rock base was an added challenge. Within the first 5min of driving on these, I noticed a major difference in pulling quality. The trailer smoothly went over dips and bumps in the road that would have originally bounced my truck all over. It’s not a 100% cure all, major bumps in the road still had some movement in the truck, but the overall change is well worth the price and amazing quality you will get. I also bought the upgraded wet-bolt kit and shackles, which I’m sure added to this great performance. If you have the original suspension, buy this now, you will be very satisfied!
Scritto da: John Reeves
Cheap bolts
The bolts are very cheap and strip out very easy.
Scritto da: dbagpiper
Excellent upgrade to our tendem axle camper
I had a little over 3000 miles on our 28' camper (GD 23BHE) when I took the plunge and installed these with a wet-bolt kit. We then took a 2500 mile trip lasting 12 days. What a difference! Things like "porpoising" of the rig from bumpy and uneven road and sway from passing vehicles were drastically reduced to almost non-existent. It really smoothed out the towing experience (Tundra Crew TRD). Install wasn't bad but I have a lot of tools so... I still took about 4 hrs a side because I was taking my time and had a couple persnickity leaf bushings that didn't want to come out. Could probably do it in 2 hrs per side.
Scritto da: Fraser
Works perfectly. Fairly easy install.
Installed this on my 2012 Timber Ridge 240RKS. Did the wet bolt kit at the same time, took about 4 hours total and it’s works great! Trailer is silent now, and seems to handle bumpy roads much better! Just don’t forget you loosen the spring mount nuts from the inside, the bolts are splined into the shackles and spring mounts.
Scritto da: Gord
They work Great !
I put a set of these on my hunting cargo trailer last year. They made such a huge difference in the ride, I got a set for my 28 ft RV trailer. I do a lot of gravel road travel. I'm looking forward to a smoother ride
Scritto da: Chris
Tows straight as an arrow
Made the trailer completely stable. No shake and tows amazing. The first upgrade to any trailer
Scritto da: Mike Como
Arrive quickly
Arrived quickly, packaged very well in factory packaging. The condition of the paint does make it look used but I think it was just thought handling in the factory. I will be installing on a 2019 apex nano 208BH. Initial fit looks perfect will lift camper 1/2-3/4” Will update once installed.
Scritto da: M Setchell
Well worth the money
Did the Morride CRE 3000 and wet bolts. The Travel trailer is only one year old, with about 3000 miles on it. The plastic suspension bushings were wore out already! I changed them out myself in my driveway easily.

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